Monday 26 April 2010

Code for motor directions

Whilst testing the prototype other noticeable issues were found and have lead to the following changes.

The original outputs to the motor drive (to turn the wheels in a specific direction) were noticed to have caused the buggy to have turned and followed a different root to what was intended by the project brief.
This was noticed particularly when testing the symbols code (particularly the middle symbol as it was found to go forwards and turn right rather than go forwards and then reverse):



I then changed the program to take into account of the new conditions:

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