Friday 30 April 2010

Project review

I found this project to be very enjoyable and interesting. I have learned a lot with respect to working in a team and building and designing a buggy.

Towards the end there were a few issues with the programming and design. This was due to the late completion of the design and lack of work done during the easter break.

As a whole I feel I could have contributed to the programming side. The programming was a weakness of mine which is why I had such a lack of involvement in that area. By being involved I could have improved my knowledge of programming and gained a lot more from this project.

Overall this project was still rewarding in many ways. The team worked well together and there were no major issues between team members. Seeing our buggy being successful on the test was very satisfying.

Top layer ideas

After it was decided the buggy would be made into two layers, the top layer was to be designed differently to the bottom.

Here were a few design sketches for the top layer:

Line Buggy Testing

The following shows the final tests on the buggy when it carries out line following:



Review

I would conclude that this module has been well informative and very practical. It allowed the group to turn an idea designed and formulated on paper and build an intelligent robot that can perform several important tasks specified by the brief.

One of the best aspects was that we managed to source the materials we needed from recycled or unwanted components, which was the original intention of producing as buggy that was as 'environmentally friendly' as possible.

It was found that the buggy showed good tracking skills as during the line following stages it managed to reach the half way point however unfortunately due to selected pauses and the curvature of the chassis it unfortunately had a natural tendency to turn towards the right. This coupled with the rear wheel caused the buggy to loose track of the magnetic tape at various points across the line.

The gap in the following picture between the motors (when it was attempted to show alignment using a ruler) shows they could not be perfectly aligned, this turning effect would be magnified by the fact that the wheels had a natural incline.



The rear wheel would need to be substituted with a more appropriate jockey wheel as during the line following it was noticed that it could easily catch itself on the slightly thicker than expected track (this problem was also noted in other buggies):



This property amplifies the turning effect and often made it difficult for the buggy to reverse as it would get itself easily jammed:



It was however an improvement on the initial rear wheel shown in the picture as agreed by the group it impeded movement due to its weight and required more power from the to obtain the desired turn.

An improvement on the program could include the use of a RAMP function on the output in order to gently increase torque in order to slowly accelerate and decelerate the buggy particularly as it approaches a corner. This will also reduce the chances of overshooting or provoking the oscillating/'hunting' behaviour that was noticed as soon as it lost the track.

Project Complete - PM's Review

The project is now completed with the final test concluded, as depicted by the Gantt chart below.



The project started off very well, and in the initial phases we accelerated beyond schedule. Unfortunately this progress was lost over the Easter holiday's, though we pulled the project back and completed it on time. In retrospect I should have accounted more for the inevitable decrease in group members output over the holidays and planned around them, though by motivating my team immediately as term resumed we were able to finish on time to a high standard.

The intended budget for this project was £0.00 which we were able to meet. All components were sourced for free as either unneeded spares or from recycling centres over the Easter holiday's.

The program worked well and much of the design was also good, though we were let down by the rear caster wheel. The original was sourced by me from Swindon Recycling Centre, and when tested it turned out to be to heavy and stiff. I made attempts to modify the wheel and also treated it with WD40 to loosen it, though the weight ultimately let it down. The wheel was replaced last minute with a homemade caster wheel which did not perform well on the line following mode as it would cause the buggy to veer off course whenever it tried to turn. If I were to do this project again, I would have sourced a light-weight pololu ball caster to replace this wheel.

The symbol reading part of the final test went smoothly, as the rear wheel did not have a chance to cause problems. The design assessment was acceptable, though the aesthetics of the design could have been improved with practise. Some of my cuts were not perfectly straight and the holes drilled by Anand caused the acrylic plates to crack in several places. This caused the final build to look a little rushed, and were a result of our limited experience using tools.

The power of the motors was also a little low. The battery pack was only just powerful enough to power the circuit and motors. As seen in other groups, if I were to repeat this project I would have designed a secondary power supply specifically for the motors.

In conclusion I feel this project went well. We scored highly in the final assessment and worked well as a team. To improve our project if I were to do it again I would have planned our schedule better around the Easter holiday's so that we could have had more time testing, installed a secondary power source for the motors, dedicated more time to ensuring the build was neat, and sourced a better rear caster wheel.

Final Build

I sourced the acrylic for the final build from a scrap bin at the university; and with the assistance of the Assistant PM, Electronics Specialist, and Chief Designer; began the build process.

The first stage was to measure the components, create a design, and to cut the acrylic to size. Sophie and I did the first stage of this, and then Sophie created the robot design shown below. I was then able to cut the boards to size.


Picture Taken By Sophie Latham

Sophie then, with advice from the team, used the component sizes to mark out where all holes that required drilling should be positioned and the boards were given to Anand, in the condition shown in the picture below, for him to drill at home.


Picture Taken By Sophie Latham

The next stage was for me to cut out the slots for the robots arms and legs from the top piece, whilst Anand wired in the circuit to the lower piece of acrylic. Once this was complete, Daljinder sanded down the acrylic components and I designed a variable spacer to be placed between the sensor array circuit and the lower sheet of acrylic. This design is depicted below and as the bolts shown are tightened/loosened, the array is raise/lowered respectively. This design keeps the circuit under enough tension to keep it in place without risking damage. There was concern raised about the heat from the circuit melting the sponge, though these were quickly dismissed considering the low voltage and frequency at which the circuits operated.


Picture Taken By Sophie Latham and Edited By Mark Hawkins

The result of these processes is shown below.


Picture Taken By Sophie Latham

Sophie then, with some advice from me, finished her design by using my electrical tape, and part of a disco ball, to decorate the face plate on the top of our robot. This was then bolted down and the final assembly was complete, as depicted in the images below.


Picture Taken By Sophie Latham


Picture Taken By Anand Bhana

The caster wheel on the back of this final design turned out not to be fit for purpose. It was too heavy and caused the batteries to drain too quickly with little movement.

After much debate amongst the team, Sandra's design for a new back wheel was chosen and implemented, creating the final design shown below that was used in the final test.


Picture Taken By Sandra Donohoe

Pictures of the final Buggy

The following pictures show a lateral view of the buggy, in particular the location of the components underneath and on top of the first layer of acrylic:







Labels were added to make it easier to connect the wires bake to their original pins as they needed to be taken appart in order to pass them through the slot that Anand created.